So all my bolts were tight. It was my throw out bearing. Replaced it and now its good. Also I used 2 quarts lucas 80w90 and a half bottle of the oil stabilizer...works magic.
I have my consult with ecutalk and a conversion cable and cant get it to connect so I am working with the company to find out why. That's awesome.
I replaced the microfilter on the valve cover T with a line going to my intake...much better.
Still running the 2 fuel pressure regulators. Still running Great.
Also found out that my gauge is in fact measuring -8/-9 PSI. It has a switch on back to switch my reading to bar and it reads -.5/-.6 which in turn is equivalent to -16/-18 In.HG.
BAM BITCH
My car is now running awesome and now my only issue is my front cover leaks under heavy load. Sounds like a job for oil resistant rtv.