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Tech Talk Technical Discussion About The Nissan 240SX and Nissan Z Cars |
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#1 |
Nissanaholic!
![]() Join Date: Nov 2007
Location: bumfuck VA
Posts: 1,825
Trader Rating: (33)
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s13 sr20det(t28), possible wg actuator issue?
hey quick question, about a week ago i switched to a hotpipe with a nipple so the wg actuator could have its own boost source and to also fix a spiking issue i was having between gears. after i did that the turbo was still quick to spool but a few days ago the turbo started to become kinda laggy so i boost leaked tested the system and fixed all of the leaks and its still doing the same thing. i was wondering if it could be the actuator going bad. i had this issue before when i had the greddy hotpipe on with a nipple as well but when i swapped back to having the wg line tee'd off of the bov line it became responsive again. im wondering if anyone had any suggestions before i pulled the trigger on buying a new actuator.
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#3 |
Zilvia FREAK!
![]() Join Date: Jun 2007
Location: San Francisco
Age: 37
Posts: 1,007
Trader Rating: (22)
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Why not test the actuator? Your already in there testing the whole system for pressure, might as well apply pressure to the actuator and see if its leaking.
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#4 |
Zilvia FREAK!
![]() Join Date: Sep 2009
Location: Midwest
Age: 35
Posts: 1,401
Trader Rating: (91)
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Running a boost controller? Could also be the culprit.
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#5 |
Nissanaholic!
![]() Join Date: Nov 2007
Location: bumfuck VA
Posts: 1,825
Trader Rating: (33)
![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() ![]() Feedback Score: 33 reviews
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i replaced the actuator with a new oem one and it seems a lil better. its did the same thing with 2 different boost controllers. i had an evcs before it crapped out and replaced it with a blitz sbc for the time being. i have the gain set on 36 iirc and it feels somewhat decent for the moment.
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