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08-05-2010, 10:10 AM | #1 |
Zilvia Addict
Join Date: Sep 2009
Location: Nor Cal
Age: 37
Posts: 720
Trader Rating: (10)
Feedback Score: 10 reviews
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Damn im curious to know what else you're going to put on there to aid the burnouts lol. any new pics by any chance? this things just too clean.
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08-05-2010, 10:37 AM | #3 | |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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Quote:
I would love that! You could cover up all of the blemishes for me, haha. I want to have Toby help me with some bride door panel fabric someday, so maybe I could make a weekend road trip out of it before the snow flies! |
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08-05-2010, 11:57 AM | #4 | |
Zilvia FREAK!
Join Date: Nov 2006
Location: Normal, IL
Posts: 1,026
Trader Rating: (12)
Feedback Score: 12 reviews
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Quote:
Ya get with him on the door cards and set something up. I've got the garage space for the car if it was a weekend thing/if you need a place to crash. |
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08-08-2010, 09:13 PM | #6 | |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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Quote:
So the weekend went like this... Friday: Left work a little early and my GReddy Type RZ BOV, flanged hot pipe, and recirculation fitting from Enjuku Racing were waiting for me- just in time! So I threw that stuff on the car- haven't installed the recirc hose yet, though. Saturday: Shane and Trevor came out to help enter my Shadowerks base map into the Power FC. It took some messing with it, but Trevor got the car running really well! We drove it around the block and checked a few things, but everything seems to be in great shape. Idle was strong and drivability was great. I ended up cruising around town a bit and everything seemed great! Thanks again to Trevor (MagicalTrevor) and Shane (Holemilk) for coming out all that way, really appreciate it guys! Sunday: My wife and I ended up going to Brighton for dinner and some dessert. The car drove really well and we didn't run into any issues, aside from a few exhaust scrapes, lol. Tuning is scheduled for Tuesday night at Monkey Wrench. Once the car is tuned, I can have a good time! Looking forward to seeing how the car does. I'll post some street pics tomorrow. Last edited by CamryOnBronze; 07-28-2017 at 01:13 PM.. |
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08-09-2010, 06:55 AM | #11 |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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haha thanks a lot! I like it without the hood too for some reason. Probably because it looked SO nasty when I got it. I never thought it would end up looking so much better...
Decided to drive it to work today since last night's outing went so well. So, the farthest trip so far is about 35 miles. That should help burn up the old gas so that I can fill it up fresh tomorrow before the tune. Couple quick cell pics: Last edited by CamryOnBronze; 07-28-2017 at 01:25 PM.. |
08-11-2010, 07:42 AM | #14 |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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I LOVE the sound of the D-Max... the sound of my exhaust combo is perfect to me, I really like it!
Well, the car is tuned! Matt at Monkey Wrench said that everything went really well for the most part, and seemed to be a pretty solid street setup. He rearranged some vacuum lines for me and installed a t-bolt clamp on one coupler I missed (I didn't buy enough, haha). The only real issues we ran into were: 1. Boost Controller- My older Blitz EBC was having issues with holding boost correctly. It would occasionally hit 2-3 psi higher than it was set for, realize it mid way through the pull, and then pull boost quickly- sometimes pulling lower than the value it was set for. Matt got the controller set up really well for me, but I will still need to play with it to sort that issue out if I can- or look into other options if not. 2. Test Pipe- Remember that strange bung on my Megan test pipe with a bolt in it? Well, the bolt ended up coming out on one of the pulls, lol. So I now have a cool exhaust whistle/leak- I'll toss it back in with some Loctite tonight and hopefully never deal with it again. If that doesn't work, I'll just have it welded shut. 3. Oil Leak- The car started leaking oil towards the end of the evening. We are not sure exactly where it is coming from, but it seems to be from the turbo area and collecting on the steering rack/ front subframe. I will have to get under the car tonight or tomorrow night and clean everything up, find the leak, and fix it. It left a lovely trail up the driveway of my new (to me) house as well, so that will be another project for me. :lol: I am hoping the clamps on the turbo drain/return are just loose or something. Here are some pics! My car was in good company at Monkey Wrench, haha: We ended up hanging out with my wife's grandparents during tuning since they live about ten minutes from the shop. Old people dig 240s... lol. So yeah- the numbers are going to read pretty high on a DynaPack dyno, but here is one of the printouts I got. I am pretty positive that this pull was done at 10 psi. We had some computer/printout issues, but the highest value I saw while I was there was 347whp at 14-15 psi. I am going to email Matt to confirm the numbers/boost settings for my reference, but it is probably right around 300whp and 275wtq on most dynos. I'll have to try it on a Mustang dyno at some point and average the numbers, haha. I am very happy with the results. I only did one pull on the way home, through most of third gear, due to the oil leak and test pipe leak, but it feels AWESOME! For sure the fastest car I have ever owned by far, so it feels pretty crazy to me at the moment- and that was at 10psi! I couldn't be more happy with the setup and the tune and service that Matt gave me at Monkey Wrench- thanks for hanging out there late to get my car done! I'll post another update by the weekend after I sort out a couple issues and get the car all cleaned up. Should be driving it a lot this weekend and hitting some meets, so it should be fun! Last edited by CamryOnBronze; 07-28-2017 at 01:20 PM.. |
08-11-2010, 08:59 AM | #18 | |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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^ thanks man!
I just confirmed the numbers with Matt at Monkey Wrench: Quote:
Not sure if other Zilvians are involved or not, but I made the top 16 in the Wiring Specialties photo contest and I am trying to make the top 8 now. If you'd like to vote, here is the link! WS Harness Set RAFFLE - TOP 16 !!! |
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08-12-2010, 07:44 AM | #24 | |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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^ Thanks guys! Yeah, I was pretty sure from my research that this setup would do about 300whp, so I am happy. Everything seems to be in order for the most part.
Quote:
I got home late last night, but I believe I managed to find and correct the oil leak. I am really lucky that I didn't have further to drive than I did- this was a nasty leak. The underside of the car is trashed, so tonight I am going to change the filter, fill the oil, and make sure everything checks out- then give the whole underside a good scrub down and cleaning. There are also some areas that could use some more undercoating, so I may address that as well. The exhaust leak is fixed now too- so hopefully it will be ready to rock for the weekend by this evening! And hopefully the trail of oil will come out of my driveway... lol. Assuming the spot I found was correct, the oil leak was from one of the turbo lines near the block. The banjo bolt was tight in the block, but this portion of the line had come loose: [Image Lost] I didn't see low oil pressure or anything on the way home, so I am hoping that everything checks out OK tonight. The oil level was just slightly above full when i left the shop, so I think it should be fine. Very close call, though! Last edited by CamryOnBronze; 07-28-2017 at 01:21 PM.. |
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08-16-2010, 08:03 AM | #30 |
Post Whore!
Join Date: Oct 2008
Location: MI
Age: 38
Posts: 3,916
Trader Rating: (131)
Feedback Score: 131 reviews
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^ WHAT!?! I responded and told him i would be there! The WIFE is wimping out, not me! lol. I just need to know the weekend so that I can mark the calendar and make sure we don't have anything planned. I am totally planning to make it out though, I'll probably find someone to ride along... but I don't think the wife wants to go.
Here are some new pics I snapped during the weekend's festivities: So I started the car yesterday to back it out to wash it, and heard a really loud squeal. Alternator belt- I was actually surprised it took that long to loosen up after breaking in. So I tightened up, feeling accomplished that my 240 issue for the day was behind me. I backed it out and started hosing it down, only to find this: Fail! These tires have two tanks of gas on them, lol. Luckily, my friend that manages a Discount Tire said it can be fixed, so I'll take it in on my lunch today and get it taken care of- then I'll be back on the road tomorrow! So annoying, haha.I spent the rest of the afternoon washing the exterior and cleaning the interior out. Last edited by CamryOnBronze; 07-28-2017 at 01:34 PM.. |
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