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Tech Talk Technical Discussion About The Nissan 240SX and Nissan Z Cars |
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#1 |
Zilvia Addict
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![]() Update for today 4/23. I pulled the upper mani off and found fuel in 3 of the runners... when i turn power on to fuel pump ecu etc no fuel drops into lower manifold.... any suggestions here ?
Update for today 4/24. Found one missing oring (inj to manifold) on injector #2 if counting from front to firewall. I replaced that and all of the others (inj to fr and inj to lower mani) with brand new orings. Put back together and fired up and still getting bog issue and 14HG Vacuum need to run a logg and then send to shadowerks - havent done this yet wanted to do a little more diagnostic before i bog him down with my problem. : ) Update for 4/30 - 5/1 Finally got Reducing coupler for a 4"od to 3"od. I am running the 4" Anti-Surge Compressor. Ordered a Spectre 4" to 3" reducer but the douchebags at Oreileys said the measurements were od but they ended by being id. Ending up going to Grovers Plumbing and Electrical for a Rubber Reducer for Piping. Sealed up just right Think i spend more time than money building the tool... I found a Boost Leak at the boost controller and that was it.. Update for Cinco De Mayo Weekend 5/3 - 5/5 * Reset Timing per spec at 15 degrees *Timing Lock at 15 degrees in Haltech *Fuel trim at 0 *Data Logg sent off to Shadowerks Video of Data Logg Session http://www.youtube.com/watch?v=02xkS9iwshQ Video of Boost Leakdown @ 20PSI http://www.youtube.com/watch?v=NhmEDjGcivs [IMG] ![]() ![]() ![]() Finished up switch panel and final wire up while i was waiting. ALSO Most Important update.....Thank you all for your insight and help, I appreciate all ! The Fuel pump and all other Accessories are wired into a ATC fuse block and Respective Relays. Ignition and Power on Switches Searched Tech Forums for issue - all info i have found leads to a few things...PCV Valve, Piston Rings,Sticky Valve,ring lands(mixed info on this one) or vacuum/boost leak, air leak on intake. Just installed Power Enterprises HEad Gasket and ARP head Studs. Head Machined at Bullet Machine with components checked. A little more info on the car - Wiring Specialties made me a new S15 Harness with all of the Haltech Sensors wired in (AIT,Wideband,Map) for easy integration. Data input and linearized - *We have set the Inj Dead times and Flow Rates Correctly *We have done the Fresh Air calibration for the wideband *Calibrated ECU for Proper Ignition Dwell times (LS2 Coils) *Calibrated for 0% Throttle and WOT calibration for the Q45 TB TPS. Current Build is 1.5 YRS in process. Issues: 14HG Steady Vaccuum at idle (good vacuum is 18-22hg @ idle) getting a ton of AIR Blowby in the Crankcase Car will run better when oil cap is off. when putting back on it boggs and wants to die Car is acting like timing is off (just got timing map done) Have Checked and diagnosed 125 for first Puff and max 140 all 4 cylinders PCV Checked and Cleaned Greddy Catch can with proper routing *No oil in intercooler piping or Turbo intake outlets Currently Running 10.5AFR @ idle (Optimum idle AFRs are 14.8-15.2) Car will not drive - SR20DET S15 *Toda 256 in/ex Cams *Haltech Plat Pro Current Map by Shadowerks Steve. *Haltech MAP AIT *Widebands by PLX and Haltech *Garret 3076r T3 *750cc injectors *Q45 TB *Aeromotive FP and FPR *Titan top mount rail *LS2 Coils MAgnecor wires *Greddy FMIC * Greddy Full 3 inch exhaust *Tial 38mm Wastegate with external dump *Oil Cooler *50MM VBand BOV *Russell SS -4 AN Lines from tank to rail/fpr Before pulling fuse box [IMG] ![]()
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert Last edited by richmond82; 05-06-2013 at 09:23 AM.. |
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#2 |
Zilvia Addict
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obviously you are running quite rich, have you looked into that as the culprit of why you're car is bogging?
At the very least you should look at the injectors and o2, although if the o2 was faulty your car would probably still run well enough to drive, just suck back the gas. Sound to me like you have one or more faulty injectors or a terrible map on the ecu |
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#7 | |
Zilvia Addict
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Quote:
I am going to run a data logg today and send to Steve At Shadowerks to watch in real time and help out. How would you recommend i test the injectors ? Make sure they are getting power and ground or through the ECU ? I am literally minutes away from pulling intake manifold and checking for any leaks (this is one thing i havent done yet) A little more info on the car - Wiring Specialties made me a new S15 Harness with all of the Haltech Sensors wired in (AIT,Wideband,Map) for easy integration. The Fuel pump and all other Accessories are wired into a ATC fuse block and Respective Relays. Ignition on Switch *We have set the Inj Dead times and Flow Rates Correctly *We have done the Fresh Air calibration for the wideband *Calibrated ECU for Proper Ignition Dwell times (LS2 Coils) *Calibrated for 0% Throttle and WOT calibration for the Q45 TB TPS. Current Build is 1.5 YRS in process.
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert Last edited by richmond82; 05-06-2013 at 12:15 PM.. |
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#8 | |
Zilvia Addict
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I have CP Pistons Rings Manley rods main studs and acl type H race bearings and thrust washers in the garage ready to be put in. Dilema - i am knee deep in this build and would like to get her running for a few months before i have the Machine Shop get to work....
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#9 |
Zilvia Addict
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One thing i havent done yet is just that - a leak down test. i need to go buy one
I havent pulled the intake manifold and checked to see if the Gasket maybe is pinched or misalligned ( i was too lazy to replace a stud on the lower intake manifold when i noticed it didnt have one. I used a bolt but thats not the best way to ensure i have proper seal.) I will update once i have completed this...
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#10 |
Zilvia Addict
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![]() You sir are lucky that it runs well for you. That low of Vacuum could mean a variety of things ?
but it runs great so no worries.... and yes my S15 is a tempermental Bitch. which is why the rebuild
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#12 | |
Zilvia Addict
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I had new SS lines made up using ATP oil restrictor for the Turbo and a 5/8 AN SS return. Oil lines go from block to oil cooler then turbo and then back to block. Coolant lines were a AHOLE to get flow and bends right with very limited room... Glad that part is over...
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#13 |
Zilvia FREAK!
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Any chance the opening at the rear of the head for the crankcase line became plugged clogged?
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Z32 with lq4 swap Desert Street Scene || Dssevents.com |
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#14 |
Zilvia Addict
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if they were leaky wouldnt i smell fuel ? Unless they arent sealing on the rail - i will do this after i check mani
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#15 |
Zilvia Addict
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I pulled mani and found fuel in 3 of the lower intake runners. I turned key to ACC and no fuel dripped into lower intake. I found one injector with no oring on it - could be the culprit for all of my headaches... will know for sure tomorrow
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert Last edited by richmond82; 04-23-2013 at 04:30 PM.. |
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#16 |
Zilvia Addict
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ACC? My fuel pump does not turn on unless my key is on RUN, but I am 100% OEM wiring - no workarounds.
If you have no o-ring on a injector it would shoot fuel all over the place. If the injectors are leaking internally, electrically or from o-rings, the fuel stays in the intake manifold. EDIT: This is for side feed, sorry I see you are top feed |
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#17 | |
Nissanaholic!
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Or the injector to rail? Assuming injector to rail, since the other would be obvious. How does fuel not spray everywhere!? Also agreed with above, did you prime the pump or just turn the acc on?- edit read the update..I like how u update the first post. Have you boost leak tested this thing?
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@UpshiftEngineering |
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#18 | |
Zilvia Addict
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#22 | |
Zilvia Addict
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We have calibrated in the Haltech Plat pro for 0 throttle and WOT the readings were 0 and 4.42% if i remember correctly The timing was set when the head was put back on post changing the Head Gasket and Studs
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#23 |
Nissanaholic!
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Boost leak test that shit!
#1 cause of low vac Super easy to do
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@UpshiftEngineering |
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#24 |
Nissanaholic!
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you must go into the haltech software and set the timing to your desired value (ie 15) in the setup section (main table), set timing lock on in the software and verify/adjust the timing with a light at the cas/distributor.
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#25 |
Zilvia Addict
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![]() its at 15.0 in the main setup tables. was shot with timing light for verification. Will need to perform this again before checking off as possibile solution. Compared to my Apexi DJetro i Love Haltech
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#27 |
Zilvia Addict
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Timing lock is enabled. I will double check tomorrow. Going to do a leak down test and boost leak test in next two days. I will update with results as this car is begging to be driven.
Thank you all for your insight and help, I appreciate all !
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#28 |
Zilvia FREAK!
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Also, on ur picture the nipple on the valve cover near the turbo, whats going on there?
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Z32 with lq4 swap Desert Street Scene || Dssevents.com |
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#29 | |
Zilvia Addict
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Quote:
Good Call. This is an old Pic before hooking back up the lines routed to Greddy Catch Can
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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#30 |
Zilvia Addict
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Update for 4/30 - 5/1
Finally got Reducing coupler for a 4"od to 3"od. I am running the 4" Anti-Surge Compressor. Ordered a Spectre 4" to 3" reducer but the douchebags at Oreileys said the measurements were od but they ended by being id. Ending up going to Grovers Plumbing and Electrical for a Rubber Reducer for Piping. Sealed up just right Think i spend more time than money building the tool... I found a Boost Leak at the boost controller and that was it..
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Drake: 95 Swapped S15SR Z32 Swapped TT 1991Vert |
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compression test, garrett, standalone, turbo |
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